ebay Motors'Â Grassroots Motorsports $2012 Challenge Race Report
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ebay Motors'Â Grassroots Motorsports $2012 Challenge Race Report

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Some more pictures from the GRM $2012 Challenge.
$2012 Challenge
9/27/12 Day Before the Competition
Just because we had the car actually driving before the competition this year doesn't mean we didn't leave things to the last minute. Â Before getting the car on the trailer we still had to finish fitting the rear bumper cover which did not fit at all because it's supposed to go on an E36. Â Making it look half way decent (from 10ft) required a lot of trimming. Fortunately I had Skitter and my dad (who flew in to come to the competition) there to help. Â Unfortunately Skitter decided that this would be a good time to stab himself in the thigh with a utility knife. Â After discussing stitching it up himself (which sounded like a terrible idea to me) he managed to drive himself to a clinic, get the cut stitched and make it back before we left for Florida.
Once we arrived in Gainsville and checked into our hotel we had one last item on the to do list before we called it a day. Â Nick and I had cut some vinyl decals a few days before at Georgia Tech and it was time to apply them. Â Nothing too fancy just a little something to get an extra half a point from the concourse judges.
 9/28/12 Day 1 Autocross & Concourse
Day 1 started early, we got to the track early, unpacked the truck, torqued our lug nuts, and finished up a couple last minute things. Â For autocross we were just going to run boost control using the wastegate spring only, which was good because we still had not gotten the EBC working properly. This arrangement gave us a peak boost of about 15psi which gives us more than enough power for autocrossing. Â
While getting ready Steve Hoelscher, one of the pro drivers GRM makes available for the autocross event, came over to chat about driving our car. Â Steve is a 6 time SCCA Solo National Champion, 25+ time SCCA Solo Divisional Champion, and the 1989 Solo Nationals Rookie of the Year making him more than capable of ringing out all that our car had to offer. Â So, with that and the fact that Iâm pretty sure no one wanted to drive our car at last yearâs competition so we considered this a great start to the day.
After walking the track and watching the first few cars run we decided to get the concourse judging out of the way so we made our way over to that area with the car. Â Concourse is not exactly where we spent much time working on while building the car to this point but itâs nice to share with other car guys what we did and why. There was a small crowd, a few judges from GRM, and a few guys from ebay motors. Â They seemed to like the car, but obviously there is nothing flashy or overly nice about the bodywork/finish of the car so we didnât expect much from the scoring in this department.
     After concourse we prepared for our autocross runs.  I would drive the first two runs as a shakedown to ensure the car was running well and that all the wheels stayed on and then we would hand over the keys to Steve⌠The challenge rules allow each entrant to have five runs and only the best of those runs counts towards your challenge score.  This would give Steve three runs to get comfortable and get the most out of the car.  Unfortunately, in my first two runs a transmission problem became painfully apparent.  Due to what is likely failed/failing synchro, shifting from third down into second proved to be extremely difficult.
After our second run we had a decent middle of the pack time but had definitely not gotten everything out of the car due to the transmission problems.  We then found Steve, explained the issue, which he was confident he could deal with, and away he went for our third run.  The following 20 minutes would prove to be the most exciting of the weekend for us.  Watching the car run around the course spitting flames out the exhaust and making all sorts of fun noises finally gave us all a sense of accomplishment.  It didnât hurt either that Steve was able to get the car from third into second without much fuss and put the car solidly in second place after his second run.  His third and final run didnât quite go as planned and he ended up wiping out most of the cones at the end of the course when he attempted to shift into third instead of riding the rev limiter.  Looking back on it, we should have just bumped the rev limiter up a few hundred rpms and he might have been able to squeeze out a couple tenths⌠oh well, next time.
  After that last run the car was on the verge of overheating so we had to do a couple slow passes up and down the road to get it to cool back down before parking it for the day and watching the rest of the autocross action.  Our second place standing stuck until the last run of an unexpected competitor. A turbocharged Jeep Cherokee surprised everyone by claiming the fastest time of the day, pushing us down to third. Itâs interesting to note that the only other car to best ours in the autocross was another Chrysler product, the âScariesâ a 1987 Dodge Aries!
So, at the end of the first day things were looking pretty good. Â We packed up the car and headed to Applebees for a much deserved meal and then back to the hotel for some rest.
9/29/12 Day 2 Drags
Coming off of our good performance the previous day we weâre hopeful we would at least be able to put down a decent drag time despite having more than a few hurdles to overcome. Â This would be my first time drag racing, as last yearâs drags were rained out and itâs just not something I had done before. Â On top of that, we had an untested electronic boost control system, autocross tires (which have a much too stiff sidewall), Â transmission problems, and probably worst of all we left the soft rear springs at home so getting off the line was going to be challenging.
My first run didnât go so well. Â I started in first gear, but thanks to our failing transmission I had to almost come to stop a few hundred feet down the track to get it into second. Â Needless to say, the et wasnât too great but the trap speed (over 100mph) showed that there was some potential there. Â A few more runs starting in second and we had some decent 14 second passes that we were happy with. Â With these out of the way it was time to start trying to raise the boost and see what we could do. Â Unfortunately our untested EBC system was not functioning as planned and we couldnât get our programming changes to make any difference in the boost numbers we were seeing.
Thatâs when we started to improvise; we pulled the boost control solenoid and hosing out and instead started poking holes in the vacuum/boost reference line that fed the wastegate. Â This is essentially the way a manual boost controller works, by introducing a controlled leak in this line it fakes the wastegate into opening at a higher manifold air pressure. Â Poking holes in a hose wasnât the most controlled way to hit our target boost of 21 psi. Â At one point we blew the line open causing uncontrolled boost and luckily the megasquirt stepped in (as programmed) and cut spark. Â To have more control over this leak we had Nick and Mike run to a hardware store and pick up a small needle valve that we added in line so we could dial in the boost. Â This worked great, although the extra boost didnât get us much more in terms of et. We ended up with a best run of 13.82 seconds which was good enough to put us in the top 10 drag times. Â With more grip off the line and some more practice the car should be able to easily get into the 12s. Â
At the end of the day we were all happy with how the car did and we had a lot of fun. Â Most of my time was spent focusing on our car and trying to get it to go faster but there was some exciting runs going on throughout the day. Â The Scaries ended up running an 11.69 after breaking and repairing a half shaft, putting them solidly in the lead. Â The Jeep Cherokeeâs best time wasnât far off of ours with a 14.04!
After packing up for the day and heading back to the hotel for some rest and a shower we headed over to the host hotel for the awards banquet. Â The banquet was a lot of fun, we had some great food and had time to meet and talk with other competitors and GRM staff. Â When it came time for the results we were very anxious to see how we placed overall. Â It turned out we placed fifth overall and considering how things went last year we were pretty darn happy with that. Â Overall, we had a great time at the competition and look forward to the next time we can compete! Â
 Special Thanks
A lot of people helped with car over the past year and there is no way the car would have made it to the competition and done as well as it did without their help.  Iâd like to say thanks for all the helpâŚ
Christian Yeager (aka Skitter)
Nick Ginga
Mike Hirsch
Valve CoverÂ
Just a few more finishing touches before it's time to head off to the competition. Â Decided to polish and paint the valve cover using some left over high heat crinkle paint. Â It came out pretty good!
Electronic Boost Control
Now that we had an adequate external waste gate it was time to fine tune and control the boost we could run. Â On just the wastegate spring, boost was peaking at around 15psi which was actually quite decent for autocross. Â However, by adding boost control we will be able to obtain more overall boost and achieve it earlier in the rev range by actively controlling the wastegate. Â
Megasquirt is easily and inexpensively modified to be able to control an electronic boost control solenoid. Â Output for the solenoid was simply routed to an unused pin on the main Megasquirt harness connector. Â We sourced a 3-port boost control solenoid from a turbo GM and plumbed it as shown in the diagram above. Â Next step is to figure out the correct Megasquirt settings and get it tuned. Â Our target is 20psi for the drags...

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Bumper Covers
One thing we have decided to do this year to make the car look a little more complete is the addition of bumper covers. Â We sourced well used bumper covers from an E36 at the local pull-a-part and proceeded to hack them up to make them fit (poorly). Â The front was cut in half sectioned and spliced back together to get the width correct. Â It also needed to be slightly trimmed to match up with the wheel arches. Â The rear is going to take much more work as the E36 has a much rounder rear than the E30. Â Hopefully we can get it fitted before the competition.